石油科技论坛 ›› 2022, Vol. 41 ›› Issue (3): 86-93.DOI: 10.3969/j.issn.1002-302x.2022.03.011

• 采油采气专刊 • 上一篇    下一篇

大庆油田井下作业清洁化与自动化技术研究与应用

王洪卫1 刘崇江1,2 姚飞1,2,3 宋兴良1,2 徐晓宇1,2 刘钰川1,2 赵骊川1,2 王鹏程1,2 马百涛1,2   

  1. 1.大庆油田有限责任公司;2.黑龙江省油气藏增产增注重点实验室;3.东北石油大学
  • 出版日期:2022-07-08 发布日期:2022-07-08
  • 作者简介:王洪卫,1975年生,2010年毕业于东北石油大学石油与天然气工程专业,博士,教授级高级工程师,主要从事采油工程技术研究与管理工作。
  • 基金资助:
    中国石油天然气股份有限公司科技开发项目“绿色安全降本增效技术研究与应用”课题3“大庆井下作业自动化与清洁作业技术研究”(编号:kt2018-18-03)。

Research and Application of Clean and Automation Technology for Downhole Service in Daqing Oilfield

Wang Hongwei1, Liu Chongjiang1,2, Yao Fei1,2,3, Song Xingliang1,2, Xu Xiaoyu1,2, Liu Yuchuan1,2, Zhao Lichuan1,2, Wang Pengcheng1,2, Ma Baitao1,2   

  1. 1. Daqing Oilfield Co. Ltd., Daqing 163453, China; 2. Heilongjiang Provincial Key Laboratory of Oil and Gas Reservoir Simulation, Daqing 163453, China; 3. Northeast Petroleum University, Daqing 163118, China
  • Online:2022-07-08 Published:2022-07-08

摘要: “十三五”期间,为改变传统井下作业“脏、险、苦、累”现状,大庆油田开展了清洁化、自动化作业技术研究与应用。按照“井液不出井、出井不落地、落地不污染”绿色作业要求,针对井下作业过程中井液出井污染环境问题,攻关形成了以井筒溢流控制为主、地面集液回收为辅的清洁化作业技术系列,累计应用20.8万井次,回收废液382.7×104m3,减少固体废物6.3×104t,清洁作业覆盖率由23.6%提升到100%。针对传统井下作业劳动强度大、安全风险高的特性,发展形成了小修、大修自动化作业技术,通过配套自动化作业装备,单队操作人员比例降低25%,年节约人工成本100万元以上,劳动强度和安全风险大幅降低。清洁化、自动化技术的发展与应用实现了井下作业安全、绿色、高效施工,推动了劳动组织方式和生产运行模式的变革。

关键词: 井下作业, 安全环保, 清洁化, 自动化, 劳动强度, 生产模式, 绿色高效

Abstract: Daqing Oilfield focused on research and application of clean and automation service technology to change the traditional downhole service conditions of formation damage, safety risk and high labor intensity during the 13th Five-year Plan period. The green service requires “no fluid out of the well, no fluid on the ground, and no environmental pollution on the ground surface”. A series of clean service technologies focusing on wellbore overflow control with the effects on surface fluid collection and recovery was developed to solve the environmental pollution issues caused by fluid out of the well. This technological series was used cumulatively for 208,000 well times, recovering waste liquid for 382.7×104m3 and reducing waste solids for 6.3×104t. The coverage rate of clean service was raised to 100 percent from 23.6 percent. The automated service technology for workover was developed in the efforts to alleviate high labor intensity and high safety risks of downhole service. Development and application of systematic automated service equipment reduced the service personnel proportion of a single crew by 25 percent, saving labor cost for more than 1 million yuan a year and dramatically lowering labor intensity and safety risks. Development and application of clean and automation technology brought about safety, greenness and high-efficiency of downhole service and promoted transformation of labor organizational mode and production operational pattern.

中图分类号: